|
News Archive 2004 Indian Point wins
high rating from NRC
Roger Witherspoon
The Journal News
November 25, 2004
The twin nuclear power plants at Indian Point have received
high marks for a safe, effective operation in their third-quarter
evaluation by the U.S. Nuclear Regulatory Commission.
The "green" rating, the highest the agency awards
in its color-coded evaluation system, means Indian Point
is considered among the best-run of the nation's 103 nuclear
plants. By year's end, it will begin receiving the minimum
level of oversight and inspections for the first time in
four years.
"It has been a slow, gradual climb for Indian Point
back to the performance levels it should be at," NRC
spokesman Neil Sheehan said. "Since 2000, they had red,
then yellow or white findings, so it was a turning point
for them earlier this year when, for the first time, they
didn't have any findings beyond green."
The agency's inspectors did write "deviation memos" when
the green rating first was issued in April, requiring a heavier
load of inspections than normal at Indian Point. The increased
inspections were needed because there still were problems
with equipment, training and procedures. The memos are still
in effect, but the number of extra inspections has been reduced
as plant performance has improved.
"There has been a gradual stepping down in oversight,
so they are not getting the baseline inspections," Sheehan
said. "They still have issues to work on, though, and
we will continue to keep a close watch on Indian Point."
The evaluation, covering the quarter that ended Sept. 30,
found some minor problems with maintenance practices at Indian
Point 2 and 3. The evaluation was released this week by the
NRC. Entergy Nuclear Northeast, which owns the plants in
Buchanan, declined comment on the evaluation.
NRC inspectors were critical of Entergy's ability to find
the causes of major equipment failures. The plant shut down
twice in September, and reduced power on a third occasion,
because of problems maintaining proper water levels in one
of the plant's four steam generators.
Brian McDermott, the NRC's lead evaluator of both plants,
said Entergy's staff "made several unsuccessful attempts
to identify the direct cause of the feedwater problems, due
to the fact that they didn't apply a very formal troubleshooting
and root cause analysis. They did things on a piecemeal basis
and didn't work together as well as they should have."
McDermott said the lack of a systematic problem-solving
system during the first shutdown Sept. 1 led to the two subsequent
interruptions at the site. But, he said, Entergy officials
learned from their mistakes and correctly evaluated the situation
when the second shutdown occurred Sept. 24. There was no
danger to the public during the incidents.
BACK TO TOP
|